Sunday, August 4, 2013

More Weekend Shots

These glossy shots were sent to me from our buddy Melinda from Galore Racing.

Thanks Melinda


Monday, July 29, 2013

Mission Old Time Drags

Well I'm officially still exhausted from our raucous weekend in Misssion B.C. for the  Langley Loafer's Old Time Drags this past weekend. This is our big outing of the year and as usual it did not disappoint in the least. The weather was perfect and the car behaved itself, clicking off consistent 11.1 passes @ 119 mph. The new motor is nothing short of mechanical art and people flock around the car in pits like flys to honey, making it a full time job explaining what the hell is happening in the land of altered wheelbase wagons. It's also fun to kick back and watch people walking by the car as they take time to try and pronounce "Chupacabra" before giving up and continuing on. 
We still have a bit of work to do in terms of chassis tuning, gear selection and some transmission tinkering but the program has a clear and decisive path that can only lead to faster e.t.s and bigger wheelstands. We had a tight crew throughout the weekend that consisted of the entire Babe's Automotive staff, so confidence was high when minor malfunctions arose (as they always do). 
Here you can watch a couple of great passes between me and our pal Steve Chase in his awesome '64 Merc pick-up. Steve is responsible for creating a straight axle specific class for us and we're forever grateful to him for lumping our wierd-ass race cars together with like minded people. I'll post more pics as they roll in but until then enjoy these videos shot by our own "Dangerous" Chris Carlson and be sure to crank the volume for maximum smile factor. 



Friday, July 19, 2013

Torque Thrusts Baby

When we realized that our 29/10.5Ws mounted to the kidney bean wheels we had hoped to use were experiencing serious interference in the rear wheel openings and our old steel Cragars up front were noticeably out of round and uber heavy, we decided that some classic looking American Racing Torque Thrust "Ds" were just the solution.

Damn if we didn't nail that one.


Thursday, July 11, 2013

The Phoenix!!!!!!!

Rising from the ashes of a devastating shop fire comes the illustrious new race motor for El Chupacabra II. So you take one semi-retired 1964 413 stocker race block with every go fast trick known to man inside, then bore it .140 over and order up some one-off pistons to achieve 13:1 compression, then you may as well add a roller cam for good measure. Port some already heavily ported iron heads in order to match the intake orifices of a brand new cross ram from A&A transmissions. Hell, we may as well port that too in order to achieve larger that max wedge size ports. Top it all off with some custom built Edlebrock 750s and we have a serious combo. This is very much the Coles notes on what's been done to this motor but we need to keep some sectrests in the name of mystery

Here we have it with velocity stacks which will need some clearancing to work.

And K&Ns for the sake of longevity.

Tuesday, July 9, 2013

A Little Racing

We made it back to Thunder Mtn last weekend after a one year hiatus and it was great to see all the familiar faces and be able to flog our new combo at a mere 4500 feet above sea level. We scored some new Hoosier slicks but unfortunately ran out of time before heading out, so we were forced to run our old cheaters that gave us so much trouble last year. So it wasn't much of a surprise when they spun like crazy off the line all weekend long. We did manage to make some traction later in the afternoon when the track was well seasoned and followed by a massive "I have a tire sponsor" burnout. Best 60' was in the 1.63 range and our best e.t. was 7.42. We're in the process of ordering up some sweet Torque Thrust wheels to cover all four corners and we'll wrap the rears in 29x10.5W steam rollers. Say goodbye to traction issues. It was a good weekend over-all giving us an opportunity to really put some test passes down on the old Maxed wedge. This motor sounds and runs better than expected. Once the chassis is better dialed in this thing will be a serious contender.
Our next outing will be the long awaited Mission old time drags on July 27/28 and we're feeling like our shit is pretty tight. The goal is high tens with some wheels in the air action. Come out and see us in the pits, you might even get to meet my mom if you're lucky. She'll be the one trying to make you eat a sandwich and potato salad.


Thursday, June 27, 2013

Alright Already



 For those of you that have been religiously checking back to see if there was a fresh blog post since last Fall, I commend you on your diligence and patience. I'm terrible at keeping secrets at the best of times so this one was a killer. After the demise of our faithful old "Blue Bullet" race motor at last years season closer, Chris and I made a hard decision to bite the bullet and get our pal Dan Dvorak to build us something special. Dan is a legendary stock racer and engine builder who has been slinging his trade since our car was new. He resides in Waldo Florida so having a 700# crate shipped coast to coast seemed unreasonable to us...therefor we decided it was a good idea. As we began scheming with Dan about our hopes and expectations from this new mill it was clear that this project was going to quickly spiral out of control. Better the project than the car though. I made haste in acquiring a retired 413 block and heavily massaged heads from our pal and racing mentor Chris Barnes. Now that we had a starting point we needed to make some big decisions about induction, oiling, compression and the like. It was important to us to keep as much of a visually appearing 1964 race motor as possible. If our car was built in 1965, which is the era of our "Funny Wagon", it would most likely have a fuel injected Hemi for power. A private race team would probably be able to procure a cross-ram Max Wedge from the previous season for half of what it would cost to get into a Hemi. We went this route. Though our iron heads are not the original "hens teeth" Max Wedge" units, they are ported beyond belief and will (according to Dan) out flow the original MW heads. The Cross-ram that we decided to use is a beautiful reproduction built by A&A Transmissions and it has also been ported to match our tricked out iron heads. Since we're not running in a stock class we decided that it was o.k. to completely rollerise the motor and add every "go-fast" trick that those poor stocker's aren't allowed. It seemed like a good idea in the scheme of things. Dan took two brand new 750 cfm Edlebrocks and completely re-worked them for our application. There is way too much going on to list here but when the dust settled and Dan broke the motor in on his stand, running 15-20 gallons of fuel through the big lung to make sure that everything was well sealed and ran like a champ. It did. Dan was beside himself with the results. This from a guy who has been building race motors his entire life. He ran it for me on the phone and the sound was unbelievable. "It sounds like a funny car" Dan says. He of course is referring to a more modern top fuel type of car. The irony is that our machine is the original "funny car". Tonight we will install the motor and hopefully fire it up.

 Let the wild rumpus begin!!!

 

Friday, October 19, 2012

Out With a Bang

Chris and I got up at an ungodly hour on Oct.7th in order to venture out to the final race of the season in Osoyoos. The weather was perfect and crisp and the turn-out was huge for this little airport/drag strip. As usual our beloved nostalgia slicks were giving us no love. We tried various pressures and volcanic burnouts carrying them right up to the lights but to no avail. Next season we will be addressing this problem but on this particular Sunday we were content to live with it. As usual we got plenty of qualifying passes but by the end of our fifth run, old Chupacabra shut down and refused to start. A quick glance at the oil guage showed no pressure. I coasted off the return road and glided to to a halt in the dust.

 End scene.

 A spun bearing is the obvious culprit but we won't know for sure until we tear it down. The ironic thing is that this was the last race for the old "Blue Bullet". This 440 has been with us since the beginning and has been a tried and true power house over the last decade. Wait a minute Pat. Why is this the last race for that mill? Well race fans, I guess you will just have to stay tuned since we have a super exciting transplant in the works that will be an all out game changer for this car and team alike. Sorry for the spoiler but I'll hold out the details until install time. Until then it's off season time for El Chupacabra where we will be doing some steering geometry refinements, fuel system upgrade and a few smaller tasks to prepare for the 2013 race season. Stay tuned